Home Viral News “Why Did You Cut Off Fuel?” – 15 Key Findings From The Air India Crash Probe Report
Key Findings From The Air India Crash Probe Report

“Why Did You Cut Off Fuel?” – 15 Key Findings From The Air India Crash Probe Report

Aviation Accident Investigation Bureau (AAIB) released the preliminary report on the terrible plane crash in happened in Ahmedabad.

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It appeared to be a typical morning on June 12, 2025, but what transpired at noon rocked the world. Under normal circumstances, Air India Flight 171, a scheduled international passenger flight, took off from Ahmedabad Airport in India to London Gatwick Airport in the United Kingdom. But nobody knew what was going to happen in the next few minutes. About 30 seconds after taking off, the Boeing 787-8 Dreamliner carrying the flight crashed. Soon after takeoff, the plane started to lose altitude while keeping its nose up and wings level.

The fact that the plane crashed into the Ahmedabad hostel block of B.J. Medical College is even more horrific. The aircraft crew reported a lack of thrust and power, resulting in a mayday call. On impact, the collision resulted in several explosions. Twelve crew members and 230 passengers were on board the plane. Except for one passenger, all were perished. In addition, the crash claimed 19 lives and left 67 more injured on the ground. Now, the preliminary report on the terrible crash was released on Saturday by the Aviation Accident Investigation Bureau (AAIB). So, let’s get to know what actually went wrong with the airplane.

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Preliminary Inquiry Report on Ahmedabad Plane Crash

1. Mid-air cutoff of fuel for both engines

At 08:08:39 UTC, three seconds after liftoff, the fuel cutoff switches for both engines activated, one second apart. According to the report, the aircraft reached its highest recorded airspeed of 180 knots IAS at approximately 08:08:42 UTC. Immediately after that, the fuel cutoff switches for Engines 1 and 2 went from the RUN to the CUTOFF position, one after the other, with a one-second lag.

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2. Confusion in the cockpit

The voice clip from the cockpit shows confusion in the last moments. According to the report, the voice recording from the cockpit reveals that one of the pilots asked to other pilot about why he cut off fuel. In response, the other pilot said he didn’t. The investigators are investigating whether a technical breakdown, an accident, or human intervention activated the switches.

3. Engine relighting attempt

The report reveals that as soon as the flight took off, pilots found that both engines were shut down. The pilots then attempted to relight the engines as per the recovered flight data. Despite several attempts to reintroduce fuel, Engine 2 did not recover, and Engine 1 showed a partial response momentarily. This malfunction prevented the airplane from maintaining thrust. Ultimately, by then, the aircraft has already lost significant altitude.

air india 171

Airways

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4. Deployment of emergency RAT

Immediately after takeoff, the Ram Air Turbine (RAT), an emergency power source that is used in the event of a power outage, was deployed. It provides a clear signal that vital systems were losing electrical power. The deployment was later confirmed via airport CCTV footage.

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5. Mayday call not verified

Just before 08:09:05 UTC, one of the pilots made a distress call, saying, “MAYDAY MAYDAY MAYDAY.” However, when the air traffic controller made an effort to verify the call sign, but got no answer. The plane crashed a few seconds later.

6. The aircraft crashed with its nose up

According to flight path analysis, the plane struck buildings close to BJ Medical College with level wings and an 8° nose-up pitch. The airplane was unable to maintain flight with neither engine providing any thrust.

plane position

Jammu Bulletin

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7. Thrust levers discovered at idle

The flight data showed the takeoff position during the flight. While the takeoff power was engaged, the thrust levers were discovered to be in the idle position following the collision. It was determined that the landing gear and flaps were in their typical takeoff settings, excluding any unusual configuration as a contributing cause.

8. The debris was dispersed 1,000 feet

The aircraft broke up over a large area, striking several structures. Engines and landing gear were among the debris scattered over more than 1,000 feet, demonstrating the impact’s severity and trajectory. Investigators used drone photography to document the scene before securing key components.

9. Experienced pilots

Another important detail on this report is that as of now, the investigators have assigned no blame to the flight captain and his co-pilot. Both are very experienced. Captain Sumeet Sabharwal had 15,600 hours of flying experience, while the co-pilot Clive Kunder had 3,400+ hours, including extensive Dreamliner training. Both were declared fit and well-rested before the flight. However, despite this, they are not ruling out the possibility of any human error.

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Captain Sumeet Sabharwal and co-pilot Clive Kunder

10. Safety advisory not followed

A 2018 FAA bulletin flagged possible risks with the locking mechanism of fuel switches. However, Air India has not performed the suggested inspections, despite Boeing issuing an optional advisory regarding fuel control switch locking mechanisms. In 2019 and 2023, the throttle control modules of the aircraft were replaced.

11. Favorable weather

The report also states that there were clear skies and light winds during the takeoff, with no abnormal weather conditions reported.

12. The aircraft was airworthy

Maintenance records show the aircraft had no mechanical issues, and the aircraft’s airworthiness certification was still in effect. The aircraft had passed all safety checks prior to departure. Fuel control was unaffected, despite a few minor Category C and D MEL (Minimum Equipment List) problems. Interestingly, there had never been any prior reports of problems with fuel cutoff switches.

Ahmedabad Plane Crash

Hindustan Times

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13. No external interference

As per the report, investigators ruled out that any bird strikes, fuel contamination, or sabotage interfered with the takeoff of the flight. Additionally, it was revealed that the fuel loaded in Ahmedabad was clean and standard.

14. Flight carries no hazardous cargo

While people initially speculated that the crash happened due to the overloading of fuel or hazardous cargo, the report denies this. The aircraft carried no dangerous goods and was operating within permissible weight and balance.

15. Recorder & ELT failures

Standard recovery techniques were unable to recover the rear enhanced flight data recorder due to its significant damage. There has also been no explanation or interim recommendation provided for why the ELT did not transmit its distress signal following the collision. It could have an impact on the efficacy of rescue and timeline restoration.

What does Air India and Boeing have to say about this report?

After the report was released, Air India declared that it is fully assisting with the inquiry. In an official statement, Air India stated,

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Air India is working closely with stakeholders, including regulators. We continue to fully cooperate with the AAIB and other authorities as their investigation progresses.

On the other hand, Boeing stated that they continue to support the investigation and will defer to the AAIB to provide information regarding AI171.

Our thoughts remain with the loved ones of the passengers and crew on board Air India Flight 171, as well as everyone affected on the ground in Ahmedabad. We continue to support the investigation and our customer… We will defer to the AAIB to provide information about AI171, in adherence with the United Nations International Civil Aviation Organization protocol known as Annex 13.

 

Meanwhile, the AAIB study confirms ongoing component inspections, post-mortem reports, and wreckage analysis. According to the study, operators and makers of GE GEnx-1B and/or B787-8 engines are not advised to take any action at this time in the inquiry. The final investigative report is anticipated to be revealed within a year.

Also read: 27 Facts About Air India Every Indian Should Know

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What do you think about these findings? Do share your thoughts with us in the comment section of this article.

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